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The mains calibration. That worked when I tried it before buying.
I could get the meter on the calibration mark when I bought it. This
time now, I measured the transformer voltage from the inside and it
was set for 190..210V while the mains here is 235V. Yet the mains
calibration pot meter was close to maximum. You are probably
confused already now, but I realized the seller might have known
this. Please learn from me, with tube testers, if you run into any
problem "the seller may have known" you should
interpret this as: "He must have known, and that's
why he decided to sell the tester. (to you). My personal experience
is, you have 95% chance on this, and the other 5% is for cases where
a repair is easy to do. So most of the time I find the defective
spot with unsuccessful repair attempts clearly visible. Well, then
I know what I have to do,
because usually I succeed to repair this, the tester is fine
again.
TEST:
I adjusted the fuse board mains for the setting of 230...250V. Now,
with 235Vmains as we had on that moment, I should be able to set
the meter on the calibration mark with the "SET~" SWITCH, and with
235V it should be one of the last settings, clockwise.
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It
didn't work. The calibration mark
could not be reached with the SET~ switch now. I could only reach it
I set it back to 190..210V. So what did this stinky seller do....
he just set the tester for 190..210, and that way, with 230V he
could force the needle to the Calibration mark. Thus "fixing" the
problem with the non-working mains calibration.
Look
at this picture. This is as far as I could get it, with the SET~
switch all to the right. This may
mean, one of the three transformers are damaged, but I was lucky,
they were still fine.
Then I put in a calibrated Moving
coil meter in series with the meter, and the problem got clear. The meter needed 35uA for a full scale, and
it is a 30uA meter. An AVO is really only precise when all things
are within tolerance, and there is no way to work around. So if a
resistor is 10k+/- 2% there is no need to have a 1% resistor, but
don't try it with 3% if you want the whole tester to be accurate.
The most amazing thing is R36, which must be 200Ohm +/- 0.5%. I
tried it, and adding in parallel a 20k resistor to R36 will reduce
the meter reading with 5%. So for this resistor I am going to do a
"zero" percent calibration. More about this later. R36 sets the
internal impedance of the tester, and messing around by the
previous owner with it was part of the dirty job by the seller of
the tester. More about R36 later.
Now at first, I assumed the
meter magnetism must have gone down. With some meters there is a
way to adjust this. So I opened the meter, and out came the reason
for the 35uA full scale needed instead of 30uA. |

 Sorry
for the hand made sketch, but this shows best where the friction
comes from. The jewel-needle joint is in reality much finer than
dawn here.
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The whole inside was tweaked and changed in some
attempts to increase the sensitivity. Unfortunately things don't
work that way, and he gave up on it, leaving behind the meter as is.
To get the tester "repaired" still, the seller just set the tester
to 190..210V, and of course now at
230V you can reach the calibration
mark easily. So that's what he did. Now all voltages inside were too
high of course. He messed around with all other calibrations points
inside, even messed with the factory calibration, that you are not
supposed to touch. Somehow he managed to make the tester
"acceptable", and ready for sales. That's when I bought it.
The meter was damaged by over current. Other as
what many think, this will not burn the coil. You can not burn a
coil with 300uA, though this is 10x more current that normal. 300uA
is not enough for developing any heat, but there will be another
kind of damage at 300uA: This will violently hit the needle
against the end of the scale, and this will deform the coil.
Specially since (very often) the electrolytic meter protection
capacitor has gone high impedance over the years. Such deformations
can be seen easily seem under a strong lens, and fixed perfectly,
since the coil is very soft, and becomes trapezoidal shape. This is
really easy to correct , when the coil is removed. All it needs to
be is a square shape again. However, it requires complete complete
desoldering of the hairsprings, re-adjust the pivot jewels and
re-build the whole meter in fact. It's not very difficult, but you
can do things wrong very easy, and the meter is gone.
Also one of the pivot jewels had jumped out. That is
normal when the meter is badly unbalanced, the side fore on the
jewels becomes too high. These are pretty large size, and can easily
be removed. I took the opportunity to clean them also. The previous
person put oil on them, but this is wrong. The oil will give
capillary problems, and if adjusted well, there is no friction
anyway, since a well balanced needle is suspended by the hair
springs mainly. The jewels have almost no force on it, and no
friction at all. Anyway, the attempt to oil them, tells me, he was
aware of the friction.
A badly balanced coil has side forces on the jewels,
which depend on the angle, and this gives the infamous scale
unlinearity, and friction. Mmmm it's really as easy as that, but you
do need to practice a little bit on some old meters, that you would
not need any more. The Ebay price of a new meter is 450 Euro
(yes!). So better not damage your meter, and you can praise your
tester when you have a perfect meter inside. |
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Balancing of the
meter. If the coil is nicely in shape, it moves in the
middle of the magnetic gap, regardless the rotation angle. This is
elementray for good linearity, together with balancing of the needle
for vertical operation. I was able to re-adjusted the coil's shape
nicely symmetrical again, so original shape, and the meter is almost
in balance again. Final balancing needs to be done still.
First, without the circular pivot springs, you
have to set the pressure force on the sapphires, such that friction
is close to zero, yet the coil is stabile in place. This is a
balancing act, you can only do without the pivot springs. So you
need to find exactly that point where friction begins, and then
re-adjust just that tiny fraction below it. The needle as you will
see now has a small play, like approximately 0.2mm at the end of
the needle tip. It's a little bit like a rattle, when you shake it.
It's just this fraction of play you need, and this means the axis is
caught by the jewels, but without pressure on it. Once the springs
are in, the needle will be better fixed more tightly, since they
give hold in all directions. (Not just circular, but vertical also)
Next is to balance the needle, still without the
hairsprings. In the upright position, it"fell over" to the right
when it was above 70mA on the scale. It fell by itself to the end of
the scale. It is interesting to see with how large force the needle
falls over. It sort of really falls over. So unlinearity resulting
is probably a lot. As you can understand, it is just THIS effect
causing unlinearity. So if the meter is indicating " 70mA" on the
scale correct, it would indicate "100mA" on a lot less than full
scale.
If the balance is good, you can tilt the meter
forwards or backwards, and tap it, and the needle may not move, yet
if you do move it by hand it has zero friction. So this is without
the pivot springs. You out the needle in any RANDOM position, and
then you hold the whole meter in and random position, and the needle
will not move. Now is so, the meter is balanced.
If done, very gently tape a construction on the
scale of some thick paper, to hold the needle at zero, yet not bend
the needle in any direction. Now, with the meter in the normal use
position (for AVO Mk4 that is upright) solder the pivot springs back
in. |
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Luckily the coil itself was in perfect condition
still, because that I could not repair. Though I read a story in
the internet about somebody fixing the coil of a Hickok. This AVO
coil has even thinner wire.
This balancing requires very good mathematical
understanding, to get it done with three counterweights, each
interfering with the other. Well after a lot of adjusting, it was
done.
I took the opportunity to remove some magnetic
particles from the magnet, re-seal the glass, and add a dust
catching tape inside. This tape is of a kind, I have personal
excellent experience with, as I can say it will not loose it's
"stick" after minimum 15 years with air exposure. How do I know? I
had an old roll of double sided tape tape, in my drawers all of
those years, and sticks still as new. (Compay called TESA)
After final assembly this meter was a "dream" again!
It works as perfect as new, and linearity is absolutely perfect. So
with this meter, the mains calibration pot meter was within range
again.
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I checked now the Ohms Meter function of this
tester. It was excellent. I Just put back in the same picture here.
The tester has a 50 Meg Ohms Meter, which is the outer scale. It is
used when you set it on leakage. The scale stops at 25Megm but if
you look carefully, you can estimate a 50 Megs reading. Normal
multi meters work with a 9V battery, but this one here works with
appr 220 Volt DC. Which you need indeed, because leakage, corona,
creepage, all these things appear at high voltage and hot filaments.
To test it, just connected a know resistor from the A1 link to the
and A2 link, and on leakage "A1" and "A2" you must now measure this
resistance value EXACTYLY. If not, you have more work to do.
The highest precision resistor I have is 10 Megs.
The needle comes exactly on "10". PERFECT. This proves many of the
inside circuitry to be good now, including the meter. Though the
meter has to be tested as a separated unit also.
Conclusion: A
quality panel meter is a work of technical art. Specially such
sensitive ones as 30uA @ 3250 Ohms. Never try to "improve" a bad
meter by adjusting the pivot jewels. They are factory adjusted with
highest precision. They do not loose adjustment other than by coil
damage. If you change something with the pivot screws, you change
the position of the axis, and then the pivot springs develop a force
in the direction along the axis, which gives friction. So the only
thing is a full procedure as described here, or you make things
worse. |
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Grid Voltage error
(Repair)
Now comes the grid voltage repair. With this
setting, there is a small overlap with the settings wheel. So when
the range is: 0 to 5 (+10) as picture here, you can
set it from 10 to 15 Volt on the red scale. The next higher range
is 0 to 5 (+15). so you can set it from15 to 20 Volt.
TEST: You can set
15.0 Volt with either scale, and the reading on the panel meter must
be fully identical. Also when you flip from the red to the white
scale. Any differences can only come from the resistor divider
network, the pot meter linearity, and the mounting of the dial wheel
to the pot meter This mounting is a permanent factory calibration.
It didn't work. Obviously the
factory setting had been changed by the seller, the reason I found.
One of the resistors in the divider network had been overheated and
the paint was a bit burned. The seller discovered this as well,
because this resistor had been cut loose with one end, to measure
it. So did I, and it was 4% off, instead of maximum 1%. The seller
just left it in. He must have seen the paint burn, but he must have
thought 4% deviation was fine, not checking the tolerance from the
manual. . Or not have a 1% ohms meter. Whatever the reason, he left
the resistor in, and instead choose to screw around with the
factory calibration. This is the position of the dial wheel on the
potentiometer. I use this
table I made myself to check it. I do the calibration with a
scope, this is more precise as the procedure in the manual. Whatever
your choice, if you use the Excel table, whatever setting on the
"Grid Volt" is must produce this, and if not there is work to do.
After this comes the calibration with the pot meters
at the side. That is the user's calibration, not the factory
calibration. Mind you, the previous owner has been screwing around
with the factory calibration. |
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Here you see a black shrink sleeve, and inside is
a selected array of metal foil resistors, which together have
exactly the required value if 2500 Ohms +/- 1%. I think like this it
looks nicely as original. All others resistors of the grid voltage
switch were still excellent. So this is MOST likely how the meter
got damaged, by a tube with a grid to cathode short circuit. You can
discuss about it, if this is a tester's failure or an operator
failure. Probably they skipped the "shorts" test. It is just this,
what AVO is warning against. Anyway after replacing the resistor, it
was more needed than before to do the factory calibration. The best
way is by an oscilloscope, which is better as in the service manual.
After checking another Mk4, that was never worked on, I found how to
select the set points. It was kind of obvious. The service manual
explains how to use a voltmeter instead, which is easier to do, but
will not give the same nice result. After this was done, the Vg
dial performed EXACTLY as expected. Now when I set 15V on two of the
scales, the meter reading is identical. It was the wrong reading,
but at least identical, and it was so for all (nine) scales like
this. Another step forward :) |
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REPAIR PART FINISHED - NOW COMES THE
VERIFICATION This tester is so
precise, it will outdo the Amplitrex AT1000 |
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So now the tester is working good, and I wanted to
see what it can do. These curves you see here are from a NOS 6SN7,
taken with the Amplitrex AT1000 computer. As we will later see, the
precision of this 60 years old AVO MK4 tester will outdo the
Amplitrex, which is possible since the Amplitrex is not very high
resolution.
Yet, first now we need to see with the AVO where we
are at all. The numbers underneath the vertical lines of the AT100
graphs correspond with the lines in an unusual way, as more things
a bit unusual with the AT1000 tester. Anyway the values are taken
correctly, but you need to get the numbers from the curves by
penciling in the lines you need.
I will replace these
curves later by the Sofia curves, which I can directly read data
from without having to estimate the test points, and besides the
Sofia gives transconductance at any test points I choose.
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Verification of the results:
So we are going to need the values at 150V, 200V
and 250V, and check a few grid lines. You can click on the curve to
see the details. As you can see, this AVO Tester reproduces the
Amplitrex AT1000 values. What is interesting the grid voltage of the
Amplitrex is given with less resolution as the AVO. The Amplitrex
will jump from 3.5V to 3.6 (lack of resolution) whereas with the
AVO you can at least estimate on the scale the distance between 3.5
and 3.6. So you can read 3.55 from the AVO scale.
Plate =100V, -Ug=3.5V, Result 2.3 mA
Plate =100V, -Ug=5V, Result 0.45mA Plate =100V,
-Ug=6.5V, Result 1.8mA Plate =100V, -Ug=3.5V, Result
4.4mA
Conclusion: The
tester is in perfect condition. I have been verifying it's function
with the Amplitrex AT1000. Actually I really have come to the
conclusion, it is better to verify the Amplitrex with a mint
condition AVO Mk4. In some planned work, I am going to do so.
Meaning I want to produce a really absolutely "known" tube, and pass
it on to several testers. |
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Sorry
for the not so nice picture quality, but they are made with a
CANON EOS 1000 camera. |